View Single Post
Old 09-22-2014, 06:36 PM   #13
blubaustin   blubaustin is offline
 
Join Date: Aug 2014
Location: Tempe, AZ
Posts: 4
Send a message via AIM to blubaustin Send a message via MSN to blubaustin Send a message via Yahoo to blubaustin Send a message via Skype™ to blubaustin
tinker

Was just wanting to tinker, I got the "screws" out by taking it to a local motorcycle shop, the mechanic just laughed pulled out some little pliers by snap on and removed them, drilled out my jet to a 88. Bought a uni filter, going to be getting a shutoff valve instead of the vacume operated pump, removed the pairing system, removed the big restriction in the exhaust that I think was caused by poor welding. The 88 though seems like its running lean, should I up it to a 90?
  Reply With Quote